Another interesting project for us is the electric conversion of a King Motors KSRC-002. Ours was bought from Heat Hobby of Miami, FL. Out of the box, the only thing that needed to be assembled was the spoiler. Thankfully, we won't be using it. Inspecting the role cage and the transmission shaft we found some rust. This is not really a nice thing to find on your brand new model. Oh well, it will probably get replaced. Since this is an electric conversion, the first thing that I did was hop onto every HPI forum and King Motors discussion that I could find.
Several guys are using huge current setups, 200A or more. That may be necessary, we will see. I do not think they were using as many cells in serial as we intend to. Our plan is to run 9s2p or 9s3p, we also only want to be able to dash. the conversion we are running will be about getting it set up, and then moving toward the longest running build possible. Out of the box, we can see a bunch of things that do not make sense in a racing vehicle. Ok, probably not a race ready device out of the factory.
Why would you use 0.125" (3mm) steel as your chassis? Cars do not use 3mm of steel in many structural places. It can hold up with a person standing on it. One of our first projects will be to replace the chassis with an Aluminum one. This should take out about 2lbs (1kg) without any stress. Another interesting choice, which is clearly about cost is the roll cage mounts that are plastic. It is my opinion that the plastic knuckles are where the cage breaks not the quarter-inch (6mm) steel tubing. Which was also poorly finished and rusted in one of the welded joints. If King Motors reads this, please do some inspection of the parts before they leave the factory.
The fuel tank was pulled out along with the engine. a few bolts and it removed cleanly. Next time, why bother buying a full setup, go roller chassis. Forum after forum said the FM radio that they ship with it sucks. I have to say that we did have some interference on our little test stand. I could see where this would be an issue. So I yanked it out and replaced it with a composite capable 6ch Spektrum unit which we use in our planes. It is a great 2.4GHz DSM-2 radio. There are two-channel versions if you prefer.
The throttle servo and steering servos are crap, but useable. One part that is a bit challenging was the clutch. Not the clutch bell, but the clutch on the drive flywheel. Several places lauded designs that keep it in, noting that the clutch helps reduce the biting nature of the electric motors' torque curve. Anything to keep the wheels hooked up is better. Just make sure that you put the pin in first, othwerise you cannot get it through the hole with the shoe. You will need a piece of wire to go through the eye on the pin and above the retaining plate to keep the pin from falling through the hole. It is not hard to fix, but it is annoying.
The steering servo was replaced with a nice metal-bearing quarter scale unit. Our HB unit is faster, digital and stronger than the factory version. There is no reason not to use digital anymore, I hear that there were some issues in the beginning.
The catch with this that we found. The drive pinion that you need is a 1.5 mod. Yes, 1.5mod, the stock that came with our bell housing is a 17t. I contacted my normal strange parts connection at Impakt/Tekno RC. They are always awesome. They said that they did not have the parts in the scale, and directed me over to Monster RC. This is a reason, that I always go to them first. Customer service is not only helping them on your site, but helping them get what they need. Following their suggestion, I went over to RC Monster. They had the a selection of 1.5 mod gears. I emailed Mike at RC Monster, he responded quickly and said which parts that I needed. Again, great customer service, you can get 1.5 mod gears in a bunch of sizes from 12t-22t. They are cut for 8mm shafts, so pick up the reducers as well. RC Monster shipped my order the same day.
Friday, January 1, 2010
Adventures in Composites
The big thing that we learned in this episode is how to manage holes or penetrations. We made a male mold and were trying to decide how to mark and spot where we wanted to make penetrations called for in the fuselage.Marking the fabric was not particularly accurate, but it did work. The real answer that we saw was to make a potrusion where the penetration was.
It is easier to cut off a piece that sticks out past the piece that you want than it is to dig out material where you do not want it. Our design has four or so penetrations into the fuselage. Additional wedges of blue insulation were hacked to fit into the holes. They were not made to perfectly match, but were close. So you could easily see what you wanted to keep and cut.
Another interesting thing that we learned was the relative softness of home-owner classes of epoxy. Be aware of this. Y, is that any feature that looks liou can make a mess of your piece if you heat it too much to melt the wax. You have to pull the piece free form the molds and set them back down once the part is free. Putting it back down to the mold really helped the part retain its shape. As we pulled our parts off, we were concerned that they would not be square when we put the parts back together.
Due to some communications issues, there were some delaminations in areas that would have been better had they not occured. These anomalies were healed by forcing a needle into the void and using a syringe to fill it with epoxy. Epoxy is viscous, be aware that it is tough to dispense through a narrow needle. Voids were filled until it appeared to be full visually, pockets were no longer hollow appearing.
Molds seem to be effected strongly by Murphy's Law. Everything that could have gone wrong with our parts did. Our shape has several bays. Bays are hollows where square sides would be best. The bay that we took the time to box in with plywood came out well. The bays that had no boxing in had delaminations and other issues such as corner delaminations, non-square lay ups and twists where pieces hung on something and were not carefully managed back into place. In a bay, is the only area that we had any mold damage. It was due to pieces of cloth almost wrapping a narrow piece of mold. Had it been boxed in, the pieces would not have been able to wrap the way they did and pin the mold into place. This damage was minimal and was fixed with filling the cracks with glue and for the most part was a non-issue.
It is easier to cut off a piece that sticks out past the piece that you want than it is to dig out material where you do not want it. Our design has four or so penetrations into the fuselage. Additional wedges of blue insulation were hacked to fit into the holes. They were not made to perfectly match, but were close. So you could easily see what you wanted to keep and cut.
Another interesting thing that we learned was the relative softness of home-owner classes of epoxy. Be aware of this. Y, is that any feature that looks liou can make a mess of your piece if you heat it too much to melt the wax. You have to pull the piece free form the molds and set them back down once the part is free. Putting it back down to the mold really helped the part retain its shape. As we pulled our parts off, we were concerned that they would not be square when we put the parts back together.
Due to some communications issues, there were some delaminations in areas that would have been better had they not occured. These anomalies were healed by forcing a needle into the void and using a syringe to fill it with epoxy. Epoxy is viscous, be aware that it is tough to dispense through a narrow needle. Voids were filled until it appeared to be full visually, pockets were no longer hollow appearing.
Molds seem to be effected strongly by Murphy's Law. Everything that could have gone wrong with our parts did. Our shape has several bays. Bays are hollows where square sides would be best. The bay that we took the time to box in with plywood came out well. The bays that had no boxing in had delaminations and other issues such as corner delaminations, non-square lay ups and twists where pieces hung on something and were not carefully managed back into place. In a bay, is the only area that we had any mold damage. It was due to pieces of cloth almost wrapping a narrow piece of mold. Had it been boxed in, the pieces would not have been able to wrap the way they did and pin the mold into place. This damage was minimal and was fixed with filling the cracks with glue and for the most part was a non-issue.
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